WIMPUS
Expired Member-
Posts
1,827 -
Joined
-
Last visited
-
Days Won
34
Content Type
Forums
Blogs
Events
Downloads
Gallery
Membership & Shop
Everything posted by WIMPUS
-
Yesterday a friend came over to get the hardtop off and put soft top back on. Then done an 80mile drive. Fuel use is a lot better with the rebuild carb body's now, but pedal feel needs looking at. Next i need to also look at the rear end noises.
-
Over the easter weekend done a job for a friend.. He had a head rebuild, now fitted it. His car is very low milage and very original.. as was the head gasket etc. Found inlet and outlet was blowing. After head was on.. would not start and was flooded + cars overflowing. So monday went back, seemed fuel pressure was to much. His old pump was bad to, so i donated parts of my spare that was in the boot. Eventually his new float needles changed to the old ones.. then it seemed happy. Tuned the carbs fully and now drives well.
-
The seller I bought it from.. no reply. As i need Fox to be in good shape for next weekend and the next 2 weeks, i wanted to get it sorted asap. So another trip to Anglo Parts. Man behind the counter comes with the new pump 'these are really good ones'. I look at the box .. Q parts. I said it was the same brand of the failed one now and in 2021 when my older pump failed and bought a new one .. that failed after 100kms... also Q Parts . Sh*t quality. Looking up this brand, nothing to be found. Time to have a spare one it seems now.. I was offered by a friend from the UK an early rebuild waterpump with grease nipple for free, but seems the pullys are smaller.
-
Ffs... now waterpump weeps after 5 and a half months. Did notice a bit of coolant on the inside of the bonnet, but just had changed the thermostat to 82° one. Contacted the supplier now.
-
This weekend more tuning, mostly mixture check. Now spot on it seems. But did a small service, oil, spark plugs etc. Fitted/made better seals from between bonnet / wheelarch and bulkhead. Now bulkhead is a lot dryer.
-
Yesterday evening fitted the new rebuild carb bodys. So that means.. swapping over everything of my carbs that where on Fox and tune it again. Still needs a better look this evening, but got to work today 😅 The idle is a lot better at first sight. The old dirty and a bit worn.. Time to swap parts over.. 1 carb done, time to do the other one ! Done and then it was time to fit them again. But first.. Clean the headshield a bit better. It does have a few cracks, but holds up well. Got this many years ago via Mike Charlton and I fitted a 2nd plate behind it with spacers. I also had 1 float with a drop of fluid in it. Not bad after 46 years, lucky i had spares. But.. looked for new ones. They are not made anymore, only 'unsinkable' ones wzx1304.
-
After a visit to my uncle and his TR7, I found out the 1 wrong throttle shaft Bastuck send me is actually for an... HS6 carb. Now hopefully they will understand.
-
Got to fed up with Bastuck there awful costumer service. So had a try with the throttle shafts and disc that where to big. A drill and sandpaper did the trick for the shafts.
-
Some more cleaning up. Noticed from last year all the brackets up front where going rusty. So repainted them.
-
-
-
Yellow Spit has now got a good handbrake after fitting a new cable etc, new starter, new heater valve. Got a head out of his parts parts cars. So that can be rebuild. He has a very big oil leak at the engine no. , a bit to much. But now hes a bit shocked how much a head rebuild is 😅.
-
There was a fibreglass 'GT6' body for sale on fb a few weeks/days ago. That has a roof ! 🙃
-
Helped a friend this last sunday. He also bought 2 Spitfires. One in bits and 1 together, but been outside for years. The body wasnt that much worse then Fox was, but shockingly welded, plated over etc. But needed to work on his Spitfire that had been layed up inside for 20 years until 2 years ago.
-
Fox was playing up the last week. So.. time for a tune up. Mixture and carb balance was a bit off. Now runs well again 🙃
-
-
Thanks Theo, the oil will do it much good i think 😅. But this was the factory original mount (47.000kms). Not driven it yet myself, owner drove it last week daily when it was -6.. Because... his 16 year old Range rover doesnt start when freezing and the range of his Audi E-tron it a lot less (+ hates the car/suv). Now.. to take the front shocks off, as the car sits 1inch lower at the drivers side and doesnt feel solid when going over a speedbump. My guess is.. tired springs and shocks, again original Unipart.
-
-
-
I had the bootlock frozen up several times. For a lomg time i had played up. So got it all apart, cleaned it (lots of dirt/crud etc came out). Now it seems to work a lot better. The lock springs are becoming tired after 10 years.
-
-
Yesterday been fixing the Dolomite Sprint I used laat summer. New steering uj's (incl upgraded spit solid lower uj) and new gearbox mount. Gearbox does have a leak somewhere from above. But everything is from 1978, never been apart. Next is to look why the car leans an inch to the drivers side..
-
I have an old original, but doesnt work to. Will have a look if i can fix it.
-
Hi, does anyone know a decent switch to replace these ? I now had a few fail. Current one is failing again and is a year old. GAE191