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tom horse

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  1. The problem with it , other than the dodgy welding, was probably caused by it not being securely bolted onto something flat when the flanges were welded on. Most likely because they only used the outside bolthole as there isn't any other and rather than make a suitable clamp they just went with the one bolt. this arrangement would have allowed the inner edge of the flange to bend due the the heat of the welding. I have a similar manifold to go on my 2000 when I get around to putting the engine back in. I'll have to check before hand now, especially as I couldn't find one for a 2000 mk1 and had to tweek a GT6 MK1 manifold to fit (more heat and bending). I should learn the black art of TIG welding and make my own manifolds.
  2. It's not like it's a 10 mins drive down the road and with brexit the extra paperwork and expense makes it easier, quicker and cheaper to do it yerself. Stuff used to take a couple of days either way but now it can get held up in customs if all the 'I's aren't dotted and 'T's crossed.
  3. tom horse

    Manifold woes

    Having bought a sports manifold from a place who's name resembles an outside area you'd expect horses to be kept, It became apparent it wasn't well made, leaky welds etc. so we welded up the leaks and thought that was job done. Oh how wrong we were. Yesterday as we again tried to stop the blowing where the rear (N°4) flange meets the head by fitting yet another gasket, but first we decided to take the whole manifold off and check the trueness of the flange alignment. Sure enough both outer flanges where at an angle to each other meaning there was no way it was ever going to seal as there was gaps where both inner flange edges meet the head of about 1.5mm on N°1 & 4. So in the vice it went, one at a time we heated up N° 1 & 4 downpipes and twisted them to get the flange straight and level with each other. After getting them fairly close (less than 0.5mm gap) the offended part was bolted to a spare head using a rachet strap to pull the flanges in as the twisting had made the whole thing too wide to fit on the studs, it was then tightened down to pull it in contact with the head, all round the flanges. The pipes where then heated to red hot to relive any stress from the twisting and hopefully get rid of the last remaining 0.5mm gap. After it cooled down it was then fitted to the head using the rachet strap to pull the two flanges in , inlet refitted and all tightened down. It's so much quieter now, so quiet that you can now here the diff whine. Deep joy followed by *+°$**§% as the diff will now need to come out. One last thing if you ever have to do this make sure you either remove inlet completely or disconnect the battery because when the two met yer accelerator cable becomes one with itself. resulting is a mad dash to fabricate a replacement cable from the cable in an old Izusu you happen to have lying around. I've attached the only photo we took unless you want to see the gasket where it was blowing through.
  4. greeting all. I'm in the process of rebuild the backend of my MK1 2000, including changing diff ratio. All is well so far, except I can't find any info on setting the pinion height other than reuse the original shims, which would work with a different CW/pinion. There are a few write ups on adjusting the height but none give a figure to set it to, one actually tell you how to set it up, and says "now do some maths" but without a figure you can't. So does anyone have a figure and the best way to set the pinion height in a 2000/stag diff?
  5. Hi, Has anyone had INLET valve seats installed in a GT6 MK1. Due to the valves, inlet and exhaust, recessing into the head the PO had put shims under the rocker pedestals, otherwise there was no adjustment possible. I've had the exhaust seats done to convert to unleaded, it was while reassembling the engine I realised why they had used these hand cut brass shims, the inlets had recessed as well or perhaps they'd been cut to match the worn exhausts. Either way, the engineering company reckons they can't put inlet inserts in, as there isn't enough metal. If they try they'll have to cut into the water jacket. If anyone has had it done I can let them know it is possible. Thanks JMM
  6. I know all that but it's been cut so short you can't get enough of a grip to straighten the legs out. Which is strange when you compare it to all the other 'stuff' done to the engine during it's last rebuild. A shaped piece of feeler gauge used to try and mask a cracked head and block, no locking plate on the camshaft gear, shims under the rocker shaft to allow for the valve recession, wrong bolts holding the cam gear on (too short)and so the list goes on.
  7. Dunno, but you could nearly buy a refurbished shaft for what he wants for it. and the flange is probablyy taco shaped as well
  8. g'day, I'm in the process of rebuilding my engine and need to change the timing chain tensioner. The outer split pin is impossible to get hold of as it's been cut too short. Is there any quick ways of getting to it or will I just have to presevere with the long nose pliers and what ever else I can try to get in there? The other option is to drill the rivets out and remove the anchor plate, which would then need rivetting back on. Has anyone else came across this problem? JMM
  9. While looking for a replacement rear driveshaft/hub I found this gem...
  10.  Well it was cheaper to buy a reground crank with bearings and get it  delivered, that it was to get this one reground locally.  local price €45 per journal plus tax which is over €500. bearings extra reground one with bearings  delivered £220 unfortunatley I have to get the block bored at Monsieur   Opportuniste Vous a par les couilles Ingènierie I hope he realises I have a limited number of arms and legs otherwise I'll be using the good old myford to skim the head.  
  11. Clearly you've never worked on a Herald 🤪 Or a Fergie tractor
  12.  After trying all sorts of weird stuff to remove the rear hubs  I eventually ended up trying one of these https://www.amazon.fr/dp/B07QYFRZHW/ref=dp_prsubs_2    And the hubs all but fell off. The hydraulic part wasn't much cop as the tiny crossbar just folded up on itself, but using the normal threaded part with a piece of aluminium between the end of the threaded rod and the shaft all it took was a bit of grunting and off they came. The hub flanges didn't warp and the only damage was to one of the retaining nuts (the first one before I opted for the aluminium) I left on incase it went ballistic. It cost about £80 but it's not a one job tool and should come in handy for other stuff including the Spitfire rear hubs if I ever need to do them.
  13.  Brilliant! That what I was after.  I can now order the bearings etc and get on with rebuilding this block. The original MK1 block has a nice crack and other problems between cyls 5 + 6. The original  engine is an early block with the small journals which is a shame as the crank is in better condition than the crank in the replacement engine. The fun never ends with this 2000 MK1. I should write a book on it. From the extended clutch rod, the cracked brake drum, the ham fisted attempts at set up the carbs, the silicon used to seal the float chambers and all the other class one bodges. The bodywork is nice  though.  Thanks again for the information. JMM
  14.  Do you happen to know what size each are?
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