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Shaun5190

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Everything posted by Shaun5190

  1. I pulled off the hub today and as you say, the key had sheared off, but fortunately it had not damaged the hub or the axle! I installed a new key and replaced the other side too for good measure, now it is all back together and torqued up to spec both sides. Also had the wheels aligned so now she drives in a straight line too! Thanks for your help everyone!
  2. Hmmm, you raise a good point! I am certain i would have installed the keys, whether it wasnt seated properly or has fallen out somehow? I shall have to pull that hub back off and investigate. Thanks for the observation!
  3. Thank you for your suggestions eveyone, i have it sorted now, turns out i was double stupid!! I got down the yard last night to work on the car and try to diagnose the issue, where i started off by turning the propshaft by hand to see what happens. The gearbox and clutch held firm, however i could freely turn the prop shaft without the back wheels doing anything. I thought it must be the diff and set about removing it to see whats up. It was only by chance that just before i finished removing it i accidentally rotated one of the driveshafts with the handbrake applied... The drivshaft rotated and the hub stayed in place! Turns out i never torqued up the hub nutes and the jolt of putting it in gear freed the driveshaft from the hub. I got back over there this afternoon and finished putting everything back together, then i torqued up the hub nuts and all was well again.
  4. Hi Guppy, I do have overdrive, but it wasnt engaged at the time, i had tested it during the day and it worked fine. I havent checked the UJ but i imagine it would make a lot of noise if they had failed?
  5. Thanks Pete, Good to know someone else has had the same symptoms, I just hope it is as simple as the clutch plate being broken! I will be taking the gearbox out this afternoon and have a new clutch on order so fingers crossed that is all it needs! I was hoping to give the car a shakedown before a day out this weekend, so i have my work cut out!
  6. Hi glang, The clutch doesnt seem any different it just makes a grumbly noise and vibration when you put it in gear and try to drive, the gears seem to select just fine still just no drive, i havent tried putting in gear without pushing the clutch but not sure i want to risk it!
  7. Hi Rob, The restoration was body and most mechanical parts, however the gearbox and clutch are a few of the only original bits left! The gearbox seemed fine before the restoration and the clutch seemed serviceable, i will have to pull the gearbox out on Monday but i hope its as simple as a failed clutch plate as you suggest.
  8. Good evening all I have made a stupid and probably expensive mistake with my spitfire! I had just been out on my first drive after the restoration, got back to the yard and stupidly put the car into reverse without depressing the clutch... Crunch. Now when i put the car into any gear and lift the clutch there is a vibration but no movement. I assume i have fatally wounded the input shaft or something? Has anyone had a similar problem? (Unlikely that else anyone has been so dumb) or any recommendation for what i should do next to diagnose or fix? Thanks
  9. Thanks for the advice Clive, I haven't tightened any of the bush bolts yet for that very reason, I just need to remember to tighten everything up before driving it! I will have to try settling the spring as you suggest once it is on the road. It is the swing spring setup so hopefully camber change with the larger wheels shouldn't be an issue. I have new non adjustable spax coilovers in the front, but I thought they were the standard spring height (perhaps not) but wasn't sure if the lifting at the back would cause the front to dip? Spacers may be the way forward though if this is not the issue.
  10. Hi Guys, I need some advice on the suspension setup on my spitfire. I am now in the final stages of the rebuild and pushed it outside to start it up yesterday. The rear leaf spring is new and seems to be jacking the rear end up and causing extreme positive camber. Will this settle down over time? There isn't much more weight to add in the rear end to bring this down. Also, would this cause the front suspension to drop? The front wheels are close to rubbing on the arches but they are not height adjustable. Any help would be appreciated! Thanks  
  11. Thanks Andrew, It certainly will! Hopefully not long to go now!
  12. Thanks Conor, Its certainly taken some work to get it this far! Looking forward to getting it back on the road now. Blimey, I don't see how the car would have needed so much bodging after such a short time!
  13. Got the call Wednesday evening that the car was finally on its way home! Here she is all loaded and leaving the paint shop. And a little while later she was home! Unfortunately I didn't have time to start tinkering that evening so she was tucked away for the night. I was away at a festival for the rest of the week so I had to wait to get started. I had an extra day booked off on the Monday though so I booked to hire a van with a plan to get the engine back in. Unfortunately the weather was not on my side! so lots of waiting around for the rain to stop. This is the closest the engine has been to the car for 7 years! Whilst waiting around I installed the propshaft and bolted it up to the diff. Finally there was a decent break in the weather and I managed to manoeuvre the engine and gearbox into place and reunite it once more! I had read that it is possible to get the engine in and out with the bonnet in place, so rather than damage my new paint trying to remove the bonnet on my own I left it there. Fortunately it was quite straightforward and slotted into place easily. The only problem I have is that the rear gearbox mount doesn't seem to line up with the mounting holes as if the engine is too far forward. I ran out of time to figure that one out so will leave it for another day.
  14. Unfortunately the car was in the body shop for a lot longer than expected due to staffing issues, however it is now almost ready to come home! The bonnet and doors needed a fair bit of work to get them smooth enough to paint which is another reason it has taken a while. The underside was painted with stone-chip, then primed and finally painted with the new body colour. Needless to say it was a great feeling to finally see some fresh paint going on after such a long rebuild! Next up the lower portions of the cills and rear quarter were painted with stone-chip and then the whole thing primed ready for colour! I was getting very excited by this point to see the final outcome. First to get colour coated were the doors and boot lid, and the outcome is better than I had ever hoped for! However, the moment I had really been waiting for was to see the body in colour again. The results speak for themselves! Just the bonnet, headlamp cowls and front valances left to be painted now, and she should be coming home on Wednesday. Then the fun of reassembly can begin at last!
  15. I found exactly the same bodge in exactly the same place when I started the rebuild of my Mk3.   Good to know I wasn't the only unlucky one!
  16. The story so far... I bought my 1976 Spitfire 1500 in November 2011 in the knowledge that it needed a 'little bit of work', the engine was blowing out a cloud of blue smoke (which turned out to be worn cylinder bores and rings) and the bodywork was a bit tatty. However, in my youthful naivety I didn't appreciate the amount of rust and bodged repairs that had been carried out by previous owners (more about that later!). I had the engine out and got the block rebored, cylinder head skimmed with new valve guides and rebuilt the whole thing with new pistons, bearings, seals etc. This was my first engine rebuild so there was a steep learning curve, however the simple engine proved easy to work on! Unfortunately, in 2012, after about 2000 miles of driving with the rebuilt engine...disaster! I noticed the coolant was beginning to disappear at an increasing speed and gunk was building up on the underside of the oil filler cap and in the breather hoses. My first thought was that the head gasket may have sprung a leak, so I replaced it to find it had not solved the problem. I really didn't want to strip the engine down again, however one day I checked the oil level and there was gunk on the dipstick. Now something really had to be done! I pulled the engine and stripped it down again to investigate the issue. There were no obvious signs of a leak, so I sat the block on a bench and filled the jacket with coolant. After several minutes water started weeping from a hairline crack between the water jacket and the crankcase, so the block was now scrap! I had not had any overheating issues so I am not sure what could have caused the block to crack. Rather than trying to source a used engine for rebuild, I got a rebuilt short engine from Canley Classics for a good price and swapped over everything from the old engine. While the engine was out I decided to investigate the bodywork further as I was not sure it would pass an MOT with the rust and bodged repairs on the cills. Unfortunately I cant find any pictures from this stage of the build, however there were bodges on top of bodges on top of rusted original parts all over the place! A great example was the drivers side rear wing next to the B pillar, where rather than cut out the original panel and weld in a repair panel, a PO had welded the repair panel over the top of filler and the original rusty panel. To make things worse, the same repair had been carried out a further time, with another repair panel welded over the top of more filler and the previous repair panel. When I cut this piece out it weighed an absolute ton! This should give a good idea of the levels of bodgery I was faced with. In the end I decided it would be easier to strip the body of all the rusted/bodged panels and start again. The boot floor, rear valance, lower B pillars, inner rear quarter panels and outer arches were replaced first, with all the floors, cills and rear arches removed. A new heelboard and cross member were welded in as the originals were shot. I would have been better off finding a good body tub to start with! The next thing to go in were the new floors with the original tunnel welded on. Next the new inner cills and inner A pillar sections went in with the bonnet, hardtop and doors used to correctly position the bulkhead and get the gaps right. After that, it was time to weld the bulkhead and windscreen section back onto the body. New outer cills and rear wings went on as well. The final piece to go on were the A pillar and cill end finishers. After this the body was set to one side to work on the chassis. I started blasting the chassis at home however I just couldn't do it all in one day and as soon as it was left overnight the damp would rust the surface. I ended up sending it away and getting it blasted and powder coated by a professional! Looks much better with a decent finish on it! All the suspension parts were also blasted and powder coated ready for building the rolling chassis. Front end suspension and brakes rebuilt with new calipers, discs, pads and stainless steel hoses. Rear end rebuilt with new leaf spring, brake parts and reconditioned diff. Uprated wheel studs were added to the front and rear hubs to allow for bigger wheels in the future. The rebuilt chassis is ready to be reunited with the completed body tub! They are together at last! However this was not for long as the body was coming off to be blasted. I should have learned from doing the chassis how labourious blasting is! In the end I gave up and sent it away to be blasted and epoxy primed. Before and after, blasted and epoxy primed ready for the paint shop! Off she goes to the paint shop! And that bring us up to the present day. The car is still in the paint shop being filled and block sanded ready for primer and topcoat!
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